| Construction
Sequence for Diagonal Replacement
Stage I. For Joint Members with Damaged Diagonal
- Take readings from the six gauges to
establish reference data for future live load.
- Place predetermined live load at designated
locations.
- Take readings from the six gauges to
establish the magnitude of force change under predetermined
live load.
- Establish the magnitude of the residual
forces acting in the joint members.
Stage II. For Staged Replacement of the Diagonal
- Flame cut the inboard channel of the diagonal symmetrically
about the centerline of the web
- Monitor the readings of strain in the outboard channel
during cutting of the inboard channel. (These readings must
indicate that the residual compressive force in the outboard
channel did not exceed the force established in Stage I.)
- Cut the top and bottom lacing bars.
- Undo the inboard channel fasteners at joints.
- Remove the damaged inboard channel.
- Install the new prefabricated inboard channel.
- Place and tighten new bolts at the joints.
- Remove temporary bracing of the outboard channel to the
sidewalk stringers.
- Flame cut the outboard channel.
- Undo the outboard channel fasteners at the joints.
- Remove the damaged outboard channel.
- Install the new prefabricated outboard channel.
- Place and tighten new bolts at joints.
- Install new batten plates.
- Remove the temporary reinforcing channels from inboard
and outboard halves of the diagonal.
- Tighten all bolts and check their torque.
- Inspect the new construction to make sure that everything
is done properly.
- Remove and properly discard all construction debris and
unused material.
- Remove live load trucks from the construction area.
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On September 30, 1996 at approximately
8:10 a.m., a tractor trailer traversing the Tacony Palmyra Bridge
toward Philadelphia changed its direction abruptly, crossed into
the opposite lane and struck the downstream truss (truss B) of the
bascule span near Pier F. More specifically, the truss diagonal
9-10 was impacted.
This diagonal, 9.5 m (31 feet) long from work point to work point,
consisted of two C 380 x 50 channels, which are 380 mm deep with
50 kg/m (C 15 x 33.9, which are 15 inches deep with 33.9 lb/foot),
with webs installed vertically and tied together by 63 mm by 10
mm (2 1/2 inch by 3/8 inch) lacing bars at the top and bottom. The
point of impact was approximately 0.9 m (3 feet) above the riding
surface.
Serving as an engineering consultant for the insurance company underwriting
the Burlington County Bridge Commission, the owner of the bridge,
we were asked to review, comment on and approve all analytical and
repair procedures and to monitor their actual field implementation.
Damage Assessment
The original design drawings indicate that truss B, 9-10 diagonal
experienced 592 kN (133 kip) compressive force due to dead load,
although a more precise estimate showed 520 kN (117 kip) and 627
kN (141 kip) tensile force due to live load.
As a result of this accident:
- The diagonal was bent outward with an "inboard"
channel bent of approximately 150 mm (6 inches) and an "outboard"
channel bent of approximately 100 mm (4 inches).
- The lacing bars adjacent to the impact point
buckled and one of the lacing bar rivets at the impact point was
completely sheared off.
- The impact force propagated throughout the
entire member and caused slippage of the lacing bars relative
to the main channels, as indicated by cracks in paint around lacing
bars.
The consensus was that the damaged
diagonal had to be replaced "in kind" rather than repaired
because of the extent and severity of the channels' deformation,
buckling of the lacing bars and loss of the rivets' clamping force.
Attention then shifted to devising an appropriate construction sequence
and evaluating structural conditions at each step.
Construction Sequence and Structural Evaluation
The decision to replace the damaged member was helped greatly by
the fact that dead load and live load produce axial member forces
of approximately the same magnitude, but acting in opposite directions.
It was expected, therefore, that by placing live load in strategic
location(s), it would be possible to greatly reduce, if not totally
eliminate, the axial compression in the member. This consideration
also led to a decision to keep the bridge open to traffic.
Six strain gages were installed around joint #9 of the bottom chord
members, side diagonals and vertical post in order to:
- Make sure that the axial compression in the
member was indeed reduced or eliminated altogether
- Ascertain the magnitude of compressive force
relieved by placement of live load
- Monitor force level during staged reconstruction.
The construction sequence for diagonal
replacement was completed in two stages, shown in the accompanying
box on the next page.
Stress Monitoring during Diagonal Replacement
The basic rationale for gauging and staged stress monitoring was
as follows:
- Stresses induced by dead load are already
present in the members and, therefore, must be screened out so
as not to interfere with stress readings from special live load.
- Stresses induced by regular live load would
be measured and taken into account during the screening out process.
- Stresses induced by the special live load
would be recorded at each relevant stage of diagonal replacement
and superimposed algebraically on the background stresses produced
by dead load and regular live load.
- The residual axial forces acting in the members
could be then calculated and compared with the capacities of members
at each stage of diagonal replacement.
Table 1: Residual
Axial Forces for Each Member
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Stresses were read and recorded
at five stages of diagonal replacement, when the:
- Bridge was subjected to dead load and regular
live load (zero reading with traffic)
- Special live load was in place
- Inboard channel of the diagonal was cut completely
after the outboard channel was reinforced
- Top and bottom lacing bars were cut completely
- Damaged inboard channel was removed and the reinforced outboard
channel was carrying the load.
The strain gage readings (in psi)
were recorded and residual forces acting in joint #9 members (in
kips) were estimated (Table 1).
Successful Results
As can be seen in Table 1, the residual axial forces were reduced
sufficiently to allow safe staged replacement of the Truss B diagonal.
Subsequent trial lifting of the bascule span showed that the repairs
corrected the damage and that the bascule span was ready for routine
operations. All routine operations have continued safely.
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